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Upgrade programme
The current
wastewater treatment plant upgrading programme began in 1989. It is
being progressively modified as new technology and methods of treating
wastewater are addressed and standards required to obtain resource
consents are defined. We're planning carefully to ensure that money is
invested in the most effective way.
The purpose of the wastewater
network is to remove, treat and dispose of wastewater while ensuring
that the community has the best, most cost-effective services available.
Further upgrades are envisaged for the treatment plant to ensure
capacity to cope with the growth of our region. Initially four stages
were planned, followed by a further three stages.
Stage 1 upgrade (completed
1995)
The
first stage was targeted to immediately take the load off the oxidation
ponds and enable the plant to be operated in a manner that reduced
odours. It consisted of activated sludge reactor 1 and the associated
blower switch room building, secondary clarifier 1, Dissolved Air
Flotation (DAF) tank 1 and other associated works and cost over $11
million.
The reduction of
Biochemical Oxygen Demand (BOD) and ammoniacal nitrogen load on the
ponds was necessary to minimise the potential for odour production.
Various treatment plant processes were investigated and the activated
sludge technology was selected as the best practical option for North
Shore City.
Turbine blower units pump vast quantities of air through
a series of pipes and diffusers in the Activated Sludge Reactor (ASR). A
complex biological process results in the removal of organics. Sludge is
produced in the process and extracted and treated in the digesters.
The resulting
"mixed liquor" from the ASR gravitates to the 48-metre diameter
secondary clarifier. Residual sludge settles to the floor of the
clarifier and is swept to a central hopper and then returned to the
inlet end of the ASR where it seeds the incoming effluent.
Dissolved Air Flotation (DAF) Tank 1
Sludge wasted from
the ASR is very watery, and is thickened in the DAF tank prior to it
being pumped across to the digesters. This involves injecting air into
the liquid under pressure causing the air to be absorbed by the liquid.
When returned to atmospheric pressure in the tank, the air immediately
effervesces. The completed DAF unit is located with the blower building
to the rear. The tiny air bubbles attach themselves to sludge particles
in the liquid and lifts them to the surface where the sludge is skimmed
off.
The final effluent
in the tank flows over a V notch peripheral weir to the outlet pipe and
then onto the final stage of treatment, the oxidation ponds.
Blower Switch Room Building
This building has
two turbine blower units installed with space for two more to serve the
future activated sludge reactors.
Stage 2 upgrade (completed
1999)
The
primary objective of the stage 2 upgrade was to provide desperately
needed additional sludge treatment capacity. This allowed for more
appropriate dewatering than the old open air lagooning with its
associated odours, as well as providing a sustainable dewatered sludge
disposal option. Apart from the mechanical sludge dewatering facility it
also included a major inlet screenings facility and sludge digestion
capacity increase with digesters 3 and 4. Other works included the
secondary bypass, sludge storage and pond outlet control improvements,
and in total exceeded $16.3 million by the end of 1998. These works were
the result of the sludge management plan initiated by the council in
1994.
Inlet Screenings Building ($2.9 million)
The inlet screenings facility is primarily designed for
removing inorganic material that would affect other treatment processes
and to protect pumps and other equipment from blockages or damage. This
area of the plant also measures the incoming flow.
The screen design is a New Zealand made rotating
cylindrical stainless steel milli-screen, used in conjunction with screw
conveyors. These fine screens capture small plastics and other rubbish,
which previously passed through into the final dewatered sludge (one
reason for restricting possible beneficial re-use such as compost), and
this also assists downstream biological processes. (See the
Treating Solids section).
Digesters 3 and 4 ($5.5 million)
The existing two heated sludge digesters were heavily
overloaded. Two new digesters were built of a similar proven design but
50 per cent larger. They more than doubled the capacity of the plant's
sludge digestion allowing digesters 1 and 2 to reduce loads and allow
for future growth. They were built over two years.
Sludge Dewatering Building and Lime Stabilisation
Works
The plant had relied on open air drying lagoons. After
the digestion phase, sludge was allowed to age in the lagoons for two or
more years before being excavated out in summer. This process was a
significant source of odour.
The new mechanical sludge dewatering plant thickens and
dewaters sludge in a building where all odours can be contained and
treated. The dewatered sludge is of a consistency suitable to be trucked
off site or disposed of on site without the lagooning phase. The
decommissioning of the lagoons resulted in a significant reduction in
the level of odour.
Stage 3 upgrade
In
June 2001 the major part of the Stage 3 upgrade of the treatment plant
was completed. These improvements provide additional capacity to cope
with a population increase of 40,000 people, and to allow the trickling
filters (the original form of secondary treatment) to be decommissioned
and thereby remove a major odour source.
North Shore City’s population is expected to grow from
185,000 in 2001 to 226,000 by 2016. It is essential that any upgrades to
the plant to increase capacity also meet more stringent environmental
controls as set out in the resource consent.
The major components in Stage 3 included:
Activated Sludge Reactor
Two new activated sludge reactors, were built to be
similar in size and design to the existing reactor but capable of
nitrogen reduction. They and the refurbished reactor 1 use a form of
aeration with anoxic, aeration and reaeration zones. Two additional
blowers were installed to deliver the greater volumes of air required.
Clarifiers
Two new clarifiers were built, individually the biggest
components of the Stage 3 upgrade. These settle out activated sludge,
which falls to the bottom, and the now clear treated effluent is drained
off the top, much like the process of clarifying and decanting wine.
Each of the clarifiers holds the equivalent of 5.5 Olympic pools, and
more than triples the previous clarifying capacity. The effluent is then
piped to the oxidation ponds, where it spends an average of 30 days.
There the effects of continuing bacterial action and ultra violet
(sunlight) further polish the effluent before discharge out to sea from
Campbells Bay.
New gas and diesel engines
A 900-kilowatt generator takes methane gas from the
digester process and burns it to generate electricity to run the plant
and produce hot water. When running at full capacity, the generator
produces power equivalent to that used by a small town. The generator is
able to produce 70 per cent of the plant’s required electricity. A
500-kilowatt diesel generator was also installed at the plant as
emergency backup. The total cost for power generation was $2.5 million.
Stage 3 works
The Stage 3 works encompassed the design, construction
and an extended commissioning and maintenance period of secondary and
tertiary treatment processes and associated equipment at the wastewater
treatment plant. This has expanded capacity of processing and includes:
- two new activated sludge reactors
- two new clarifiers
- a second dissolved air flotation unit
- additional gas and diesel engine-generators
- increased capacity of the solids handling facilities
- biofilters and associated odour control facilities.
The operational capacities of the activated sludge
reactors (ASRs), clarifiers and dissolved air flotation (DAF) units were
similar to the Stage 1 works and continued the liquid treatment
processes established in Stages 1 and 2.
Primary sedimentation
The primary sedimentation tanks were upgraded with scum
skimmers and associated equipment. A new primary sludge pump transfer
system was installed with improved flow and density control systems. All
four primary tanks were then covered and a negative pressure air
extraction and odour control system installed.
Activated sludge process
The activated sludge capacity was increased by 200 per
cent (7000m³) with the construction of two new reactors and two
secondary clarifiers.
The reactors were configured as MLE (Modified Ludzack
Ettinger) tanks. Under this configuration the treatment process provides
nitrification and denitrification to achieve lower nitrogen, in the
secondary effluent. This second stage of the activated sludge process
increased the overall capacity of the plant and allowed the load to the
four existing trickling filters to be reduced from 15 ML/d to around 5
ML/d. At these flows the trickling filters provide a nitrified effluent
while during periods of high wet weather flows they will continue to
provide secondary treatment of the flow bypassed around the activated
sludge system.
The
sludge thickening plant, comprising a DAF unit, was duplicated to
provide additional capacity and plant standby capability while the waste
activated sludge pumps were fitted with variable speed drives to provide
greater control and compatible flow rates for the sludge thickening
plant. The return activated sludge pump station was upgraded to handle
the flows from clarifiers 1 and 2 with the third clarifier being served
by a new pump station.
Flow to the activated
sludge reactors and clarifiers is now controlled by new flow splitters
which enables equal distribution of the flow to the units and ensures
adequate mixing of the returned flows prior to treatment. Two new air
blowers were installed in the existing blower building to supplement the
two existing blowers. This increased the installed air blower capacity
of 24000 m³/hr to 48,000 m³/hr.
Sludge digesters
Two new sludge digesters were constructed under the
Stage 2 upgrade to provide additional digester capacity. Under Stage 3
the two older digesters were upgraded and retrofitted to a similar
standard as the new Stage 2 units. This increased their efficiency
resulting in a more robust sludge digestion process and an increase in
gas production.
Sludge dewatering
The capacity of the sludge dewatering facility,
constructed at the beginning of the Stage 2 upgrade, was increased by
installing a third centrifuge. This unit had a greater treatment
capacity than the original units due to technical developments since
Stage 2. Improvements to the sludge handling systems in the sludge
dewatering building were also made to improve sludge load out and daily
operations and maintenance.
Power generation
The Stage 3 upgrade project implemented the key
recommendations of a study to evaluate the options for on-site power
generation. These recommendations were to provide a purpose built
generation facility to include two new engine generators.
One
of the two engines is a gas engine sized to consume gas up to the
predicted gas production levels in 2012, approximately 7,000 m³/day,
with an allowance for a variation of up to 500 m³/day. The 900 RVA
generator takes methane gas from the treatment process and burns it to
generate electricity to run the plant and produce hot water. The
generator is able to produce 70 per cent of the plant’s required
electricity.
The other engine is a diesel standby unit sized to provide the balance
of the essential electrical power demand of the treatment plant. The
total eventual load has been determined as 1013 kW. The original gas
engine-generator, with a maximum output of 200 kW, was relocated and the
control and heat exchanger systems upgraded to provide emergency power
generation for the solids dewatering building. The solids dewatering
building is served by a power supply that is independent of the main
treatment plant and cannot readily be connected to the main plant
electrical reticulation system.
Stage 4
Stage 4 improvements are expected to take three years
and cost $33 million. Work started in 2002.
The main components of the Stage 4 upgrade are:
- Pond deepening to increase storage
- Construction of Pond 1 bypass pipeline
- Peakflow treatment pipelines and chambers
- Construction of Clarifier 4
- Construction of UV Treatment Plant
- Biosolids upgrade
- Construction of gravity thickeners
- Odour control
- Effluent irrigation trials
Three
main categories of improvements are underway at Rosedale as part of the
Stage 4 upgrade:
- Reducing odours
- Increasing capacity, and
- Improving the quality of effluent and biosolids
Reducing odours
The four trickling filters, which have been in service
since the 1960s, were decommissioned by end of July 2003 at a cost of
$200,000. Their treatment capacity is replaced by the extensions to the
activated sludge plant and the addition of the peak flow capacity for
the treatment plant.
Demolition of two of the trickling filters will make way
for a large biofilter, also called an odour bed, to be completed late
2003. This is a concrete tank filled with bark that neutralizes gases
from the gravity thickeners and biosolids dewatering building nearby.
Increasing capacity
The fourth clarifier that we began building early in
2002 was commissioned early 2003. This is part of the treatment process
that separates biological solids from liquid wastewater to produce a
clean, clear effluent.
So that we can cope with peak flows, e.g. after heavy
rain, we have increased the capacity of a number of pipelines around the
plant, built peak flow storage chambers and provided additional storage
by deepening parts of the ponds. The clay was used to fill the sludge
lagoons on site that are no longer required for the treatment process.
Improving
the quality of effluent and biosolids
Even though our modern plant treats the effluent to a
high quality an ultra-violet (UV) disinfection plant at the pond on the
eastern side of SH1 (pond two) was commissioned in 2003. Work began in
October 2002 on the $3 million, two-story complex. The UV plant will
enhance the final disinfection that occurs naturally in the ponds. The
water is raised from pond two, flows through an inlet, underneath a bed
of UV lamps and then out to the ocean outfall. Flows into and out of the
UV plant will be able to be controlled and measured.
We have also built gravity thickeners that increase the
capacity of the anerobic digesters by further thickening the primary
settled sludge and therefore decrease the volume.
Effluent irrigation trials are underway and the concept
is to implement a permanent system on the treatment plant site,
focussing on irrigation of planted areas and monitoring performance of
the trials.
These improvements are all part of the long term plan to
cater for our growing city and to meet the conditions of our resource
consent granted by the Auckland Regional Council, in September 2002, for
the ongoing operation of the treatment plant. |